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Guest Paper: 500kV Bushings Failures and Bushing Oil Sampling Program Monitors

Home » Technical Papers » 500kV Bushings Failures and Bushing Oil Sampling Program Monitors

Mike Lau, B.ASc, Senior Engineer
Generation Technical Services Department, BC Hydro

Abstract

In June 2001, a 500KV bushing ( CGE, type U ) failed and resulted in a catastrophic failure of a generator step-up transformer in one of our major generating facility. Moisture ingress was the primary suspected cause of failure. Since then, an oil sampling program on bushings was launched and a high percentage of bushings were found to have either high moisture and/or high combustible gases. One 230KV ( CGE Type F ) bushing was found to have high combustible gases and subsequent investigation revealed heavy tracking on the innermost Herkolite cylinder. A few other 500KV bushings ( Bushing Company Type 500HA67B ) was found to have moisture ingress through the top filling plugs. Amidst all these bushing testing and change-out activities, another 500KV ( A hybrid unit -- ABB Type O plus C and CGE Type U ) bushing failed while in service on a relatively new ( in service in 1994 ) shunt reactor in November, 2001. Two months later, another 500KV ( similar hybrid unit ) bushing on the same shunt reactor also failed and resulted a huge fire which burnt for hours.

Investigation on the failures of these hybrid bushings continues at the time of writing and no firm conclusion on the cause of failures can be drawn.

This paper provides some details on the bushing failures and oil sample results.


Introduction

Small oil volume apparatus, such as oil-filled current transformers, potential transformers and bushings contain small amount of oil which could be easily contaminated and greatly reduce its insulation integrity. The failures of these apparatus are usually explosive with ensuing fires and detrimental to both equipment and personnel.

Until recently, in BC Hydro, except for Doble testing, no other routine testing are specified for these apparatus. Oil samples had been taken from some makes of CT’s in the past but only for diagnostic purposes and oil sampling was certainly not a routine maintenance task.

However, with recent failures of 500KV bushings and poor test results on oil samples taken from other bushings, the current maintenance practices on bushings needed to be re-examined.


Background

Failure of a 500KV CGE Type U Bushing (Note : Not to be confused with GE Type U)

n June 2001, at the G.M. Shrum Generating Station, one 500KV bushing on one of the unit transformer, T4C, failed violently with all the porcelain ( both above and below the mounting flange ) blew up into pieces the size of a fist. Oil was drained out of the conservator tank through the bushing and fires started both on top and at the bottom of the tank. Fortunately, the sprinkler systems operated ( the heat was so intense that the sprinkler system for the adjacent bank also operated) and cooled down the adjacent equipment allowing the fire crew put out the fire eventually. An internal explosion was evident from the bulging and welding cracks on the tank. There were severe damages internally that the transformer was scraped. (Photos 1,2,3, and 4).

Investigation of the failed bushing confirmed a dielectric failure with the paper insulation punctured through from the center draw rod, at a location about one third of the way down from the top terminal, to the grounded capacitance tap. While the construction of the CGE Type U bushings ( manufactured by Canadian General Electric in Guelph, Ontario )was different from that of a GE type U ( ie no herring-bone inking process ), we were surprised to see the capacitance layers were made up of paper coated with some semi-conductive graphite like material. Smears of this material was evident in many places ( Photo 5 ).

The subject bushing was Doble tested in Oct 1998 and both C1 and C2 insulation power factors were "good".

No definite cause of failure was determined and external moisture ingress was the primary suspected cause.

Photo 1 : GMS Generator Step up Transformer banks

Photo 1 : GMS Generator Step up Transformer banks

Photo 2: Overview of faulted bushing on GMS T4C

Photo 2: Overview of faulted bushing on GMS T4C

Photo 3 : GMS T4C Overview of faulted bushing

Photo 3 : GMS T4C Overview of faulted bushing

Photo 4 : GMS T4 C – Removal of faulted bushing

Photo 4 : GMS T4 C – Removal of faulted bushing

Photo 5 : GMS T4C Bushing – Tracking on semi-conductive paper

Photo 5 : GMS T4C Bushing - Tracking on semi-conductive paper


Initial Oil Sampling Program

Prior to the above bushing failure incident, oil samples were rarely taken from small oil volume apparatus including oil-filled bushings. After the incident, it was decided that additional information on the condition of the bushings is needed and a small scale oil sampling program was launched. Oil samples were taken from all other 500KV bushings in GM Shrum Generating Station. The results was very alarming: Of a total of 41 other bushings (of different manufacturers including CGE, Bushing Company, and Toshiba ), 11 bushings (27%) were found to have either unacceptable DGA results or unacceptable high moisture content.

The results are included in Appendix 1.

Further investigation on those bushings with unacceptable results were carried out and detailed below.


Investigation of Bushing Problesms

Of the 11 bushings that there found bad, 8 were found to have high moisture content ( 23ppm to 72 ppm ); 3 were found to have abnormal amount of combustible gases. All 11 bushings were removed from services for further investigation and dryout .

A. High Moisture Content

A1.The GMS T4A bushing ( CGE Type U, with 62 ppm of H2O ) was removed from service and sent to Powertech Lab for partial discharge ( PD ) test. It failed the PD test. The unit was subsequently drained, dried out extensively with high vacuum and heat , refilled under vacuum. Subsequently, it passed the PD test and returned to service without incident.

A2. Other CGE Type U bushings found to have high moisture content, such as GMS T1B ( 23 ppm ), T12A ( 52 ppm ), and T14A ( 62 ppm ), were all similarly dried out extensively with heat and high vacuum, tested, and returned to service without incident.

A3. GMS T8C ( with 65 ppm of H2O ) and T9C ( with 72 ppm of H2O ) were both Bushing Company bushings, Cat # ART-500HA67B. The location and the likely causes of moisture ingress have been identified: With reference to Figure 1, moisture was found getting inside the bushings through the small oil filling plugs (Item 10) located on the top of the expansion metal can (Item13) and inside the terminal cap (Item 1). The underside surface of the oil filling plugs were found to be rusty and the surfaces inside of the terminal caps were coated with white powdery material indicating signs of moisture ingress.

Further investigation revealed that the moisture somehow managed to penetrate three lay ers of protection; namely ; the outer gasket seal for the terminal caps ( gaskets found to be brittle and cracked ); the inner gasket seal ( gasket found to be in reasonably good order, but the caps were not seating squarely due to the ends of some helical coils improperly protruding outside of their threaded holes ), and finally the sealing washers of the oil filling plugs ( washers found missing completely! ).

Other Bushing Company bushings were checked but so far none was found to have a similar problem.

The two bushings were also dried out, tested, and returned to service without incident.

FIGURE 1: VIEW OF BUSHING COMPANY BUSHING TOP ASSEMBLY
FIGURE 1: VIEW OF BUSHING COMPANY BUSHING TOP ASSEMBLY


B. Abnormal amount of combustible gases

B1. GMS T10B was found to have high combustible gases ( but only 1 ppm of C2H2 ). This CGE Type U bushing was removed from service and sent to Powertech Labs for testing. Surprisingly, it passed the PD test. However, there is a significant difference in the Dissipation Factor measured before (0.49%) and after ( 0.74%) the AC withstand test. Further investigation is pending, and the bushing will not be returned to service

B2. GMS T7B and GMS T7C – Both have high combustible gases including a fair amount of C2H2 ( 62 and 60 ppm respectively ). These two bushing were Doble tested prior to their removal from the transformer. The Doble test results are enclosed in Appendix 2. It was reported that on the GMS T7C bushing, oil was dripping out of the capacitance tap continuously when the cap was removed. The oil was black and had a burnt smell to it. This bushing failed the PD test miserably.

These two bushings, together with a third one from another station (WSN T4A), which also has high combustible gases ( 3005 ppm of C2H2 ), will be returned to the manufacturer in UK for investigation and possible refurbishment.

B3. A 230 KV bushing, CGE Type F bushing at Rosedale Substation , (ROS T1A Low Voltage bushing), was found to have high combustible gases. It was immediately removed from service. The bushing was subsequently dismantled for examination. Heavy tracking was found on the bottom end of the innermost Herkolite cylinder. See Photo 6. This bushing was scraped.

Photo 6 : CGE Type F bushing : Tracking on ht e innermost Herkolite cylinder
Photo 6 : CGE Type F bushing : Tracking on the innermost Herkolite cylinder


Expanded Oil Bushing Sampling Program

Encouraged with the success of the oil sampling program, the program has been extended to include other 500 KV bushings in all our generating stations and in some critical transmission stations.


More Failures of 500kV Bushings

As if we don’t have enough bushing problems, in November 2001, another 500 KV bushing failed on a shunt reactor at Kelly Lake Substation ( KLY 5RX5 ). The reactor is a relatively new 3-phase 135 MVAR unit put in service in 1994. Dark oil and burnt paper sprayed out from the joints between sections of the porcelain. No porcelain were broken and no significant damages to the reactor. The bushing was replaced with a new spare. All the bushings as well as the reactor were Doble tested satisfactory and the unit was returned to service in early December 2001.

Two months later, in the mid-night hours of 26 February 2002, another 500 KV bushing on the same shunt reactor failed explosively and resulted a huge fire which burnt for 4-5 hours. It destroyed the adjacent new spare bushing, a surge arrestor and caused significant damages to the adjacent circuit breaker.( see photo 7 ).

These two failed bushings were hybrid units made with ABB condenser core ( with semi-conductive capacitance layers ) and other CGE Type U components. A type problem was suspected and consequently, two other similar 500 KV shunt reactors were removed from service pending further investigation.

Photo 7: KLY 5RX5 Failure of ABB/CGE hybrid bushing.
Photo 7: KLY 5RX5 Failure of ABB/CGE hybrid bushing.


Conclusion

Failures of small oil volume apparatus, such as bushings, are often explosive with ensuing fires, and are indeed great threats to personnel and equipment. On-line monitoring equipment are readily available to monitor the integrity of bushings by means of unbalanced neutral current, leakage current, power factor etc. However, it would be difficult, if not impossible, to justify economically, on-line monitoring equipment on every bushing.

s demonstrated in this paper, oil testing for DGA and moisture content prove to be a good compliment to other routine testing to provide additional information on the integrity of bushings.

It would also be desirable that a guide or a standard be established for the acceptable gas level limits and interpretation of the DGA results.


Appendix 1: Dissolved Gas in Oil Results in Bushings

STN

UNIT

PH

DATE

C2H2

C2H4

C2H6

CH4

CO

CO2

H2

H2O

N2

O2

VOLUME

GMS

T1

B

20-Jul-01

<

1

2

15

600

1348

81

23

91308

4775

9.81%

GMS

T1

C

20-Jul-01

<

<

2

10

704

1107

123

10

97893

2116

10.20%

GMS

T1

A

11-Oct-01

<

20

45

17

315

1357

382

4

65714

351

6.82%

GMS

T2

A

06-Oct-01

<

<

15

6

39

1019

5

8

78300

4704

8.41%

GMS

T2

B

06-Oct-01

<

1

10

7

45

1126

6

7

81282

3224

8.57%

GMS

T2

C

06-Oct-01

<

<

10

9

80

1443

31

4

85336

270

8.72%

GMS

T3

A

06-Oct-01

<

<

11

7

71

1737

14

46

74533

2730

7.91%

GMS

T3

B

06-Oct-01

<

<

10

6

57

1341

5

6

80362

2624

8.44%

GMS

T3

C

06-Oct-01

<

2

58

27

214

1898

15

25

57074

1935

6.12%

GMS

T4

B

04-Jul-01

<

<

1

9

597

1173

116

3

80684

1729

8.43%

GMS

T4

A

04-Jul-01

<

3

2

9

568

4828

27

62

76905

3537

8.59%

GMS

T5

C

04-Oct-01

<

1

4

8

90

2589

3

9

75005

1617

7.93%

GMS

T5

A

04-Oct-01

<

<

6

8

73

1055

2

7

70142

2615

7.39%

GMS

T5

B

04-Oct-01

<

1

4

10

145

1756

38

8

79320

402

8.17%

GMS

T6

B

18-Sep-01

<

13

6

3

106

1598

25

5

60017

24002

8.58%

GMS

T6

A

18-Sep-01

<

2

56

66

238

2393

3

7

37855

7439

4.81%

GMS

T6

C

18-Sep-01

<

14

7

21

556

2620

145

3

62248

1984

6.76%

GMS

T7

B

05-Sep-01

62

1862

302

790

932

6413

407

4

58684

6843

7.63%

GMS

T7

C

05-Sep-01

60

367

115

276

259

1128

853

5

54601

383

5.80%

GMS

T7

A

05-Sep-01

<

1

15

25

219

757

442

3

66739

6088

7.43%

GMS

T8

C

22-Sep-01

<

2

16

31

337

1530

404

65

58803

2531

6.37%

GMS

T8

B

22-Sep-01

<

1

34

49

94

479

314

4

49937

572

5.15%

GMS

T8

A

22-Sep-01

2

6

47

32

78

854

298

5

48412

1744

5.15%

GMS

T9

A

22-Sep-01

<

4

64

40

162

1118

265

8

79732

706

8.21%

GMS

T9

C

22-Sep-01

<

4

31

30

221

1335

894

72

65444

853

6.88%

GMS

T9

B

22-Sep-01

<

7

49

28

359

3263

35

13

79760

4358

8.79%

GMS

T10

A

15-Aug-01

<

2

2

12

931

1915

12

5

53334

3185

5.94%

GMS

T10

B

15-Aug-01

1

263

216

638

800

5993

1172

6

57785

905

6.78%

GMS

T10

C

15-Aug-01

<

2

5

27

585

1733

44

7

90869

1196

9.45%

GMS

T11

C

26-Aug-01

<

1

1

4

405

632

71

9

64862

2489

6.85%

GMS

T11

A

26-Aug-01

<

1

1

5

588

903

144

10

71113

1257

7.40%

GMS

T11

B

26-Aug-01

<

2

1

3

334

573

70

7

41533

1753

4.43%

GMS

T12

A

30-Aug-01

<

1

1

4

488

2910

94

52

64272

2465

7.02%

GMS

T12

C

30-Aug-01

<

2

2

3

427

1981

127

11

69358

1691

7.36%

GMS

T12

B

30-Aug-01

<

1

1

6

538

638

72

10

57308

1310

5.99%

GMS

T13

A

30-Oct-01

<

<

1

5

448

474

54

2

55436

1300

5.77%

GMS

T13

B

30-Oct-01

<

1

3

6

483

1571

51

3

84235

1610

8.80%

GMS

T13

C

30-Oct-01

<

<

2

5

243

444

24

4

65088

3709

6.95%

GMS

T14

A

14-Nov-01

<

2

3

6

815

2216

68

62

84741

1007

8.89%

GMS

T14

B

14-Nov-01

<

2

2

10

1181

3085

12

4

64593

7670

7.66%

GMS

T14

C

14-Nov-01

<

2

2

6

786

2240

71

3

81460

3632

8.82%

ROS

T1-X

A

22-Oct-01

2096

1583

293

845

495

4425

854

64

84398

9755

10.47%

WSN

T2

A

14-Nov-01

3005

2681

307

1579

189

433

5520

3

46993

7498

6.82%


Appendix 2: A Double Test Result of GMS T7B Bushing

result sheet
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